In this study, landfill leachate was treated by using the sequencing batch reactor (SBR) process. Two types of the SBR, namely non-powdered activated carbon and powdered activated carbon (PAC-SBR) were used. The influence of aeration rate and contact time on SBR and PAC-SBR performances was investigated. Removal efficiencies of chemical oxygen demand (COD), colour, ammoniacal nitrogen (NH(3)-N), total dissolved salts (TDS), and sludge volume index (SVI) were monitored throughout the experiments. Response surface methodology (RSM) was applied for experimental design, analysis and optimization. Based on the results, the PAC-SBR displayed superior performance in term of removal efficiencies when compared to SBR. At the optimum conditions of aeration rate of 1L/min and contact time of 5.5h the PAC-SBR achieved 64.1%, 71.2%, 81.4%, and 1.33% removal of COD, colour, NH(3)-N, and TDS, respectively. The SVI value of PAC-SBR was 122.2 mL/g at optimum conditions.
Two new applications for sequence treatment of mature (stabilized) landfill leachate, that is, cationic resin followed by anionic resin (cationic/anionic) and anionic resin followed by cationic resin (anionic/cationic), are employed and documented for the first time in the literature. Response surface methodology (RSM) concerning central composite design (CCD) is used to optimize each treatment process, as well as evaluate the individual and interactive effects of operational cationic resin dosage and anionic resin dosage on the effectiveness of each application in terms of color, chemical oxygen demand (COD), and NH(3)-N removal efficiency. A statistically significant model for color, COD, and NH(3)-N removal was obtained with high coefficient of determination values (R(2)>0.8). Under optimum operational conditions, the removal efficiency levels for color, COD, and NH(3)-N are 96.8%, 87.9%, and 93.8% via cationic/anionic sequence, and 91.6%, 72.3%, and 92.5% via anionic/cationic sequence, respectively. The experimental results and the model predictions agree well with each other.
Lignocellulosic biomass has been widely recognised as a potential low-cost source for the production of high added value materials and proved to be a good precursor for the production of activated carbons. One of such valuable biomasses used for the production of activated carbons is palm shell. Palm shell (endocarp) is an abundant by-product produced from the palm oil industries throughout tropical countries. Palm shell activated carbon and palm shell carbon molecular sieve has been widely applied in various environmental pollution control technologies, mainly owing to its high adsorption performance, well-developed porosity and low cost, leading to potential applications in gas-phase separation using adsorption processes. This mini-review represents a comprehensive overview of the palm shell activated carbon and palm shell carbon molecular sieve preparation method, physicochemical properties and feasibility of palm shell activated carbon and palm shell carbon molecular sieve in gas separation processes. Some of the limitations are outlined and suggestions for future improvements are pointed out.
In this work, the influence of pyrolysis temperature on the physicochemical properties of palm oil mill sludge biochar (POSB) and its adsorption properties towards cadmium (Cd) and copper (Cu) was investigated. Characterization experiments suggested that POSBs' surface functional groups play the major role in the adsorption process. POSB pyrolyzed at 400 °C showed the best characteristics for Cu and Cd removal. Adsorption study indicated that contact time and shaking speed enhances the adsorption capacity of POSB. It was affirmed that pH adjustment is not necessary for POSB to adsorb Cu and Cd. Mechanism studies fitted well with Langmuir and Pseudo-Second Order model. Thermodynamic parameters indicated that the adsorption was spontaneous, endothermic and correspond to chemical adsorption. The highest uptakes of Cu and Cd were recorded at 48.8 mg/g and 46.2 mg/g respectively. This work verifies that the temperature used for palm oil mill sludge (POS) pyrolysis and adsorption condition played the most prominent role in Cu and Cd removal from aqueous solutions.
Landfill leachate is a heavily polluted and a likely hazardous liquid that is produced as a result of water infiltration through solid wastes generated industrially and domestically. This study investigates the potential of using psyllium husk as coagulant and coagulant aid for the treatment of landfill leachate. Psyllium husk has been tested as primary coagulant and as coagulant aid with poly-aluminum chloride (PACl) and aluminum sulfate (alum). As primary coagulant, the optimum dosage and pH for PACl were 7.2 and 7.5 g/L, respectively, with removal efficiencies of 55, 80 and 95% for COD, color and TSS, respectively. For alum, the optimum conditions were 11 g/L alum dosage and pH 6.5 with removal efficiencies of 58, 79 and 78% for COD, color and TSS, respectively. The maximum removal efficiencies of COD, color and TSS were 64, 90 and 96%, respectively, when psyllium husk was used as coagulant aid with PACl. Based on the results, psyllium husk was found to be more effective as coagulant aid with PACl in the removal of COD, color and TSS as compared to alum. Zeta potential test was carried out for leachate, PACl, alum and psyllium husk before and after running the jar test to enhance the results of the jar test experiments.
This study analyzes and compares the results of leachate composition at the semi-aerobic Pulau Burung Landfill Site (PBLS) (unaerated pond and intermittently aerated pond) and the anaerobic Kulim Sanitary Landfill in the northern region of Malaysia. The raw samples were collected and analyzed for twenty parameters. The average values of the parameters such as phenols (1.2, 6.7, and 2.6 mg/L), total nitrogen (448, 1200, and 300 mg/L N-TN), ammonia-N (542, 1568, and 538 mg/L NH(3)-N), nitrite (91, 49, and 52 mg/L NO(2)(-)-N), total phosphorus (21, 17, and 19 mg/L), BOD(5) (83, 243, and 326 mg/L), COD (935, 2345, and 1892 mg/L), BOD(5)/COD (0.096,0.1124,0.205%), pH (8.20, 8.28, and 7.76), turbidity (1546, 180, and 1936 Formazin attenuation units (FAU)), and color (3334, 3347, and 4041 Pt Co) for leachate at the semi-aerobic PBLS (unaerated and intermittently aerated) and the anaerobic Kulim Sanitary Landfill were recorded, respectively. The obtained results were compared with previously published data and data from the Malaysia Environmental Quality Act 1974. The results indicated that Pulau Burung leachate was more stabilized compared with Kulim leachate. Furthermore, the aeration process in PBLS has a considerable effect on reducing the concentration of several pollutants. The studied leachate requires treatment to minimize the pollutants to an acceptable level prior to discharge into water courses.
The treatability of stabilized sanitary landfill leachate via synthetic anion exchange resin (INDION FFIP MB) was investigated. An ideal experimental design was conducted based on central composite design using a response surface methodology to assess individual and interactive effects of critical operational variables (i.e., anionic dosage; contact time; shaking speed) and pH on treatment performance in terms of color, chemical oxygen demand (COD), suspended solid (SS), and turbidity removal efficiencies. Optimum operational conditions were established as 30.9 cm(3) anionic dosage, 90 min contact time, 150 rpm shaking speed, and pH 3.1. Under these conditions, the color, COD, SS, and turbidity removal efficiencies of 91.5, 70.3, 93.1, and 92.4% were experimentally attained and were found to fit well with the prediction model. According to these results, stabilized leachate treatment using INDION FFIP MB could be an effective alternative in the administration of color, COD, SS, and turbidity problems of landfill leachates.
This study evaluated the effectiveness of Fenton's technique for the treatment of semi-aerobic landfill leachate collected from Pulau Burung Landfill Site (PBLS), Penang, Malaysia. The Fe2+ or Fe3+ as catalyst and H2O2 as oxidizing agent are commonly used for the classical Fenton's reaction. In present study, the effect of operating conditions such as pH, reaction time, molar ratio, agitation rate, feeding mode and Fenton reagent concentrations which are important parameters that affect the removal efficiencies of Fenton method were investigated. Under the most favorable conditions, the highest removals of 58.1 and 78.3% were observed for COD and color, respectively. In general, the best operating conditions were pH = 3, Fe = 560 mg L(-1), H2O2 = 1020 mg L(-1), H2O2/Fe2+ molar ratio = 3, agitation rate = 400 rpm and reaction time = 120 minutes. The results highlighted that stepwise addition of Fenton's reagent was more effective than adding the entire volume in a single step. Excessive hydrogen peroxide and iron have shown scavenging effects on hydroxyl radicals and reduced degradation of refractory organics in the landfill leachate.
Landfill leachate is one of the major contamination sources. In this study, the ability of synthetic ion exchange resins which carry different mobile ion for removing color, chemical oxygen demand (COD), and ammonia nitrogen (NH(3)-N) from stabilized leachate was investigated. The synthetic resin INDION 225 Na as a cationic exchanger and INDION FFIP MB as an anionic exchanger were used in this study. INDION 225 Na was used in hydrogen form (H(+)) and in sodium form (Na(+)), while INDION FFIP MB resin was used in hydroxide form (OH(-)) and in calcium form (Cl(-)) form. The results indicated better removal of color, COD and NH(3)-N by using INDION 225 Na in H(+) as compared with Na(+) form, while no performance differences were observed by using INDION FFIP MB in OH(-) or Cl(-) form. Applying cationic resin followed by anionic resin achieved 97, 88 and 94, percent removal of color, COD and NH(3)-N. The residual amounts were 160 Pt-Co, 290 mg/L and 110 mg/L of color, COD and NH(3)-N respectively.
In the present study, Electrochemical Oxidation was used to remove COD and color from semi-aerobic landfill leachate collected from Pulau Burung Landfill Site (PBLS), Penang, Malaysia. Experiments were conducted in a batch laboratory-scale system in the presence of NaCl as electrolyte and aluminum electrodes. Central composite design (CCD) under Response surface methodology (RSM) was applied to optimize the electrochemical oxidation process conditions using chemical oxygen demand (COD) and color removals as responses, and the electrolyte concentrations, current density and reaction time as control factors. Analysis of variance (ANOVA) showed good coefficient of determination (R(2)) values of >0.98, thus ensuring satisfactory fitting of the second-order regression model with the experimental data. In un-optimized condition, maximum removals for COD (48.77%) and color (58.21%) were achieved at current density 80 mA/cm(2), electrolyte concentration 3,000 mg/L and reaction time 240 min. While after optimization at current density 75 mA/cm(2), electrolyte concentration 2,000 mg/L and reaction time 218 min a maximum of 49.33 and 59.24% removals were observed for COD and color respectively.
The objective of this study was to investigate the performance of employing Fenton's reagent in the advanced oxidation of ozone to treat stabilized landfill leachate in an ozone reactor. A central composite design (CCD) with response surface methodology (RSM) was applied to evaluate the relationships between operating variables, such as ozone and Fenton dosage, pH, and reaction time, to identify the optimum operating conditions. Quadratic models for the following four responses proved to be significant with very low probabilities (<0.0001): chemical oxygen demand (COD), color, NH-N, and ozone consumption (OC). The obtained optimum conditions included a reaction time of 90 min, 30 g/m³ ozone, 0.01 mol/L₂H₂O,0.02 mol/L Fe²⁺, and pH 5. COD, color, and NH₃-N removal rates of 79%, 100%, and 20%, respectively, and 0.18 kg O₃/kg COD OC were obtained. The predictions correspond well with experimental results (COD, color, and NH-N removal rates of 78%, 98.5%, and 19%, respectively, and 0.29 kg O₃/kg COD OC). This method reduces the treatment time and improves the treatment efficiency relative to a previously published method that used Fenton's reagent prior to ozonation.
As the ponding system used to treat palm oil mill effluent (POME) frequently fails to satisfy the discharge standard in Malaysia, the present study aimed to resolve this problem using an optimized electrocoagulation process. Thus, a central composite design (CCD) module in response surface methodology was employed to optimize the interactions of process variables, namely current density, contact time and initial pH targeted on maximum removal of chemical oxygen demand (COD), colour and turbidity with satisfactory pH of discharge POME. The batch study was initially designed by CCD and statistical models of responses were subsequently derived to indicate the significant terms of interactive process variables. All models were verified by analysis of variance showing model significances with Prob > F < 0.01. The optimum performance was obtained at the current density of 56 mA/cm(2), contact time of 65 min and initial pH of 4.5, rendering complete removal of colour and turbidity with COD removal of 75.4%. The pH of post-treated POME of 7.6 was achieved, which is suitable for direct discharge. These predicted outputs were subsequently confirmed by insignificant standard deviation readings between predicted and actual values. This optimum condition also permitted the simultaneous removal of NH3-N, and various metal ions, signifying the superiority of the electrocoagulation process optimized by CCD.
Domestic wastewater has been generated massively along with rapid growth of population and economic. Biological treatment using sequencing batch reactor (SBR) augmented with palm oil fuel ash (POFA) was investigated for the first time. The performance of POFA in enhancing biological treatment of wastewater has not been tested. The porosity property of POFA can improve SBR efficiency by promoting growth of mixed liquor suspended solids (MLSS) and formation of larger flocs for settling and facilitating attachment of microorganisms and pollutants onto POFA surfaces. The properties of POFA were tested to identify morphological properties, particle size, surface area, chemical compositions. Four SBRs, namely SBR1, SBR2, SBR3 and SBR4 were provided with aeration rate of 1, 2, 3 and 4 L/min, respectively. Each reactor was augmented with different dosages of POFA. Optimum aeration rate and POFA concentration were identified by the performance of SBRs in removing chemical oxygen demand (COD), ammoniacal nitrogen (NH3-N) and colour from domestic wastewater. The results showed the most efficient COD (97.8%), NH3-N (99.4%) and colour (98.8%) removals were achieved at optimum POFA concentration of 4 g/L in SBR and aeration rate of 1 L/min. The study also found that higher aeration rate would contribute to the smaller specific size of flocs and decrease the pollutant removal efficiency.
The aim of the current study is to evaluate the effectiveness of combined persulphate with hydrogen peroxide (S2O8(2-)/H2O2) oxidation as a post-treatment of biologically treated palm oil mill effluent (POME) for the first time in the literature. The removal efficiencies of chemical oxygen demand (COD), ammoniacal nitrogen (NH3-N), and suspended solids (SS) were 36.8%, 47.6%, and 90.6%, respectively, by S2O8(2-) oxidation alone under certain operation conditions (i.e., S2O8(2-) = 0.82 g, pH 11, and contact time 20 min). Nevertheless, the combined process (S2O8(2-)/H2O2) achieved 75.8% and 87.1% removals of NH3-N and SS, respectively, under 2.45/1.63 g/g H2O2/S2O8(2-), pH 11, and 20 min oxidation. Moreover, 56.9% of COD was removed at pH 8.4.
It was found that with replenishment, powdered activated carbon (PAC) in the membrane bioreactor (MBR) would develop biologically activated carbon (BAC) which could enhance filtration performance of a conventional MBR. This paper addresses two issues (i) effect of PAC size on MBR (BAC) performance; and (ii) effect of sludge retention time (SRT) on the MBR performance with and without PAC. To interpret the trends, particle/floc size, concentration of mixed liquor suspended solid (MLSS), total organic carbon (TOC), short-term filtration properties and transmembrane pressure (TMP) versus time are measured. The results showed improved fouling control with fine, rather than coarse, PAC provided the flux did not exceed the deposition flux for the fine PAC. Without PAC, the longer SRT operation gave lower fouling at modest fluxes. With PAC addition, the shorter SRT gave better fouling control, possibly due to greater replenishment of the fresh PAC.
Landfill leachate is one of the most recalcitrant wastes for biotreatment and can be considered a potential source of contamination to surface and groundwater ecosystems. In the present study, Fenton oxidation was employed for degradation of stabilized landfill leachate. Response surface methodology was applied to analyze, model and optimize the process parameters, i.e. pH and reaction time as well as the initial concentrations of hydrogen peroxide and ferrous ion. Analysis of variance showed that good coefficients of determination were obtained (R2 > 0.99), thus ensuring satisfactory agreement of the second-order regression model with the experimental data. The results indicated that, pH and its quadratic effects were the main factors influencing Fenton oxidation. Furthermore, antagonistic effects between pH and other variables were observed. The optimum H2O2 concentration, Fe(II) concentration, pH and reaction time were 0.033 mol/L, 0.011 mol/L, 3 and 145 min, respectively, with 58.3% COD, 79.0% color and 82.1% iron removals.
This study investigated the electrochemical oxidation of stabilized leachate from Pulau Burung semi-aerobic sanitary landfill by conducting laboratory experiments with sodium sulfate Na(2)SO(4) (as electrolyte) and graphite carbon electrodes. The control parameters were influent COD, current density and reaction time, while the responses were BOD removal, COD removal, BOD:COD ratio, color and pH. Na(2)SO(4) concentration was 1 g/L. Experiments were conducted based on a three-level factorial design and response surface methodology (RSM) was used to analyze the results. The optimum conditions were obtained as 1414 mg/L influent COD concentration, 79.9 mA/cm(2) current density and 4 h reaction time. This resulted in 70% BOD removal, 68% COD removal, 84% color removal, 0.04 BOD/COD ratio and 9.1 pH. Electrochemical treatment using graphite carbon electrode was found to be effective in BOD, COD and color removal but was not effective in increasing the BOD/COD ratio or enhancing biodegradability of the leachate. The color intensity of the treated samples increased at low influent COD and high current density due to corrosion of electrode material.